My 2009 D4 engine 278 when running well is lovely, but continues to show problems, The last one was the water hose came off a coupling on the outdrive The VP dealer did not fit it properly , so the cooling system was deprived of water when on the plane. Sorted now ( took me over 3 hours to replace the coupling/ fit the hose, only 2 bolts and hands cut to shreds.
Factory bodge, the shift cable, ; its specified as needing a 15 foot cable. They used a 16 foot one and did a crude bonding bodge for the actuator to move it a foot or so The VP dealer relocated it to the original position. Shift issues.
I was going to give up DIY maintenance, but the quality of professional maintenance seems very poor here so its DIY again.
|